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    陈猛, 徐昌学, 余世杰. 某井钻采时扶正器接头断裂原因[J]. 机械工程材料, 2020, 44(9): 92-98. DOI: 10.11973/jxgccl202009017
    引用本文: 陈猛, 徐昌学, 余世杰. 某井钻采时扶正器接头断裂原因[J]. 机械工程材料, 2020, 44(9): 92-98. DOI: 10.11973/jxgccl202009017
    CHEN Meng, XU Changxue, YU Shijie. Fracture Cause of Centralizer Joint of a Well in Drilling and Mining Operation[J]. Materials and Mechanical Engineering, 2020, 44(9): 92-98. DOI: 10.11973/jxgccl202009017
    Citation: CHEN Meng, XU Changxue, YU Shijie. Fracture Cause of Centralizer Joint of a Well in Drilling and Mining Operation[J]. Materials and Mechanical Engineering, 2020, 44(9): 92-98. DOI: 10.11973/jxgccl202009017

    某井钻采时扶正器接头断裂原因

    Fracture Cause of Centralizer Joint of a Well in Drilling and Mining Operation

    • 摘要: 南海西部某井在钻采作业时,一支扶正器在接头内螺纹处发生断裂。采用宏观检查、化学成分分析、微观形貌分析、力学性能测试、有限元模拟等方法对其失效原因进行了分析。结果表明:该扶正器接头断裂模式为疲劳断裂,疲劳裂纹起源于接头螺纹牙底;扶正器本体外径减小、螺纹牙底应力增大是其发生失效的主要原因;建议优化底部钻具组合,采用扶正器+钻铤+扶正器的组合,有效避免扶正器螺纹接头处产生较大的应力集中。

       

      Abstract: In drilling and mining operation of a well in the west of the South China Sea, a centralizer broke at the internal thread of joint. The fracture reason was analyzed by macroscopic examination, chemical composition analysis, microscopic morphology analysis, mechanical property test and finite element simulation. The results show that the fracture mode of the centralizer joint was fatigue fracture, and the fatigue crack originated from the thread root of the joint. The decrease of centralizer body outer diameter, and the increasing stress at the joint thread root were the main reasons for the failure of the centralizer. It was suggested that the combination of bottom drill tools should be optimized, and the combination of centralizer, drill collar and centralizer could effectively avoid the relatively great stress concentration at the threaded connection of centralizer.

       

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