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    熊勇, 李永斌, 陈昌达, 吴萍, 李巍. 压气机整流导向叶片开裂故障分析[J]. 机械工程材料, 2013, 37(7): 107-110.
    引用本文: 熊勇, 李永斌, 陈昌达, 吴萍, 李巍. 压气机整流导向叶片开裂故障分析[J]. 机械工程材料, 2013, 37(7): 107-110.
    XIONG Yong, LI Yong-bin, CHEN Chang-da, WU Ping, LI Wei. Cracking Failure Analysis of Compressor Rectifier Guide Vane[J]. Materials and Mechanical Engineering, 2013, 37(7): 107-110.
    Citation: XIONG Yong, LI Yong-bin, CHEN Chang-da, WU Ping, LI Wei. Cracking Failure Analysis of Compressor Rectifier Guide Vane[J]. Materials and Mechanical Engineering, 2013, 37(7): 107-110.

    压气机整流导向叶片开裂故障分析

    Cracking Failure Analysis of Compressor Rectifier Guide Vane

    • 摘要: 某型号发动机在工作570~600 h后, 出现了5起TC11合金压气机整流导向叶片开裂故障, 通过对叶片裂纹进行宏、微观检查, 断口分析, 化学成分分析及材料力学性能测试, 确定了裂纹的性质及产生原因, 并提出了相应的改进措施。结果表明: 故障叶片上的裂纹为起始应力和扩展应力都较小的疲劳裂纹; 疲劳裂纹的产生与材质无关, 装配应力、发动机工作时产生的共振应力在裂纹源区产生应力集中是导致疲劳裂纹产生的主要原因。通过边界倒圆及在工艺内控制装配间隙, 可以延缓疲劳裂纹的萌生。

       

      Abstract: After a certain type of aero-engine worked for 570-600 h, five times of cracking fault happened in it′s compressor rectifier guide vane made of TC11. Using macrography and micrography, fracture analysis, chemical analysis and mechanical property test, the cracking mechanism and causes were determined, and the corrective measures were also put forward. The results show that the crack in the failed vane was fatigue crack whose initial stress and propagation stress were small. Occurrence of the fatigue cracking was not related to the material. The stress concentration in the crack origin area, including assembly stress and resonance stress generated during the engine running, was the main reason of fatigue cracking. Rounding the edge and controlling assembly space in the process can delay fatigue crack initiation.

       

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